madness i tell you complete
-
- Posts: 14
- Joined: Fri Feb 13, 2004 11:37 am
starter gear bushing failure
A few days I posted thinking my one-way clutch on the starter gear had
failed. It turns out that it was the bushing on the starter gear that
failed, causing it to seize to the crankshaft.
Here are some photos for anyone interested.
shaft with the starter gear in place (rotor removed):
http://jeffwight.gotdns.com/gear.jpg
shaft with remnants of the bushing after peeling the bushing off:
http://jeffwight.gotdns.com/shaft.jpg
failed bushing after peeling it off:
http://jeffwight.gotdns.com/bushing
As for cause of failure, I can only assume that I got some grit or
gunk in there when I reassembled after swapping out my doohickey (my
doohickey and spring were fine by the way).
Any words of wisdom on removing the bushing residue from the shaft?
I'd really like to clean this up without tearing the whole thing down
and removing the crankshaft.
Any donor bikes out there willing to sell me a starter gear and starter?
Thanks,
-Jeff
-
- Posts: 90
- Joined: Fri Mar 08, 2002 9:13 am
starter gear bushing failure
down and removing the crankshaft.> As for cause of failure, I can only assume that I got some grit or > gunk in there when I reassembled after swapping out my doohickey (my > doohickey and spring were fine by the way). > > Any words of wisdom on removing the bushing residue from the shaft? > I'd really like to clean this up without tearing the whole thing
starter?> > Any donor bikes out there willing to sell me a starter gear and
Did you account for the woodruff key when you pulled the rotor? It could have jammed itself between the rotor and the starter gear if you did not align it perfectly when reassembling after the doohickey swap. This could have caused the striations visible on the bushing. The woodruff key might have been consumed if you didn't find it. It happened to me and ate my starter...the one way gear was OK though. Richard Korpela A15 Chapleau,ON> > Thanks, > > -Jeff
-
- Posts: 14
- Joined: Fri Feb 13, 2004 11:37 am
starter gear bushing failure
--- In DSN_klr650@yahoogroups.com, "kelpo2001" wrote:
The woodruff key was in its groove when I pulled the rotor and had no visible wear marks on it, so I don't think that is what happened. I'm kind of stumped at this point and will be very paranoid when I'm ready to put it all back together. Thanks, -Jeffq3> Did you account for the woodruff key when you pulled the rotor? It > could have jammed itself between the rotor and the starter gear if > you did not align it perfectly when reassembling after the doohickey > swap. This could have caused the striations visible on the bushing. > The woodruff key might have been consumed if you didn't find it. It > happened to me and ate my starter...the one way gear was OK though. > Richard Korpela > A15 > Chapleau,ON
-
- Posts: 457
- Joined: Sat Mar 29, 2003 10:18 pm
starter gear bushing failure
--- In DSN_klr650@yahoogroups.com, "Jeff Wight" wrote:
It> --- In DSN_klr650@yahoogroups.com, "kelpo2001" wrote: > > > Did you account for the woodruff key when you pulled the rotor?
if> > could have jammed itself between the rotor and the starter gear
doohickey> > you did not align it perfectly when reassembling after the
bushing.> > swap. This could have caused the striations visible on the
It> > The woodruff key might have been consumed if you didn't find it.
though.> > happened to me and ate my starter...the one way gear was OK
no> > Richard Korpela > > A15 > > Chapleau,ON > > The woodruff key was in its groove when I pulled the rotor and had
I'm> visible wear marks on it, so I don't think that is what happened.
ready> kind of stumped at this point and will be very paranoid when I'm
Jeff, I have a theory about this, asa similar failure happened to me after doing the doohickey on my '87 KLR. In that case, the two surfaces on the inside of the rotor and the starter ring gear that mate up with a thrust washer, were badly gauled and chewed up. I had to replace both the rotor and starter ring gear, though I'm hoping a machinist friend will be able to dress the surfaces up and I can reuse the parts in a project bike. Prior to the failure, I remember very carefully putting the thing together, wiping it down with clean lint-free rags, and then assemblying and torqueing properly. The woodruff key was in the slot, and everything was as it should be, but still the binding, gauling, and damaged to the parts. In retrospect, I think it was the fact that the parts were DRY, as in not coated with either OIL, or assembly lube, that caused the failure. I believe these parts are only splash lubricated, and since that failure, have done 7 more doohickeys, and I now make sure each and every one of this is 1. FIRST WIPED CLEAN with rags 2 THEN DRIPPING FRESH WITH OIL. 3. Then assemble as usual. In that lot of 7, I have had no failures of any kind. hope that helps, MarkB> to put it all back together. > > Thanks, >
-
- Posts: 529
- Joined: Sun Oct 13, 2002 5:32 pm
starter gear bushing failure
On Sun, Apr 18, 2004 at 05:58:12AM -0000, dumbazz650 wrote:
Note that you *don't* want to do this to the inside of the rotor; the torque on the rotor-holder bolt is supposed to give you the correct press-fit with the mating surfaces *dry*. I agree that it makes sense to get the inside of the starter gear good and oily, but you do want to wipe the end of the shaft dry after putting the starter gear on, at least if you want to press the rotor into place the way Kawasaki specifies. FWIW, I've been told that for certain other bikes, Kawasaki does specify assembly lube for the installation of the rotor. But not for ours. I think Jeff's looking for advice on how to get the bushing remnants off the shaft in his bike and how to polish it back to smooth roundness. I'm not sure what the right way to do the polishing is (I didn't do it myself when this happened to my bike, and the guy who did it was sufficiently wizardly that I would hesitate to guess how he did it; the surface was *perfect* when he was done). Valve grinding compound, maybe, or some other very fine wet abrasive, on a cloth? Thor> > Prior to the failure, I remember very carefully putting the thing > together, wiping it down with clean lint-free rags, and then > assemblying and torqueing properly. The woodruff key was in the slot, > and everything was as it should be, but still the binding, gauling, > and damaged to the parts. > > In retrospect, I think it was the fact that the parts were DRY, as > in not coated with either OIL, or assembly lube, that caused the > failure. I believe these parts are only splash lubricated, and since > that failure, have done 7 more doohickeys, and I now make sure each > and every one of this is > 1. FIRST WIPED CLEAN with rags > 2 THEN DRIPPING FRESH WITH OIL. > 3. Then assemble as usual.
-
- Posts: 3355
- Joined: Sat Dec 15, 2001 3:37 pm
madness i tell you complete
Well might have figured out why my bike has been starting so easy as
of lately..
Pulled the Air Filter cover off... "ACK" is the only word I can use..
Between the filter and the box I must have pulled out 1/2 pound of dirt.
Filter was almost completely packed with oily dust and some sand, the
bottom of the box was covered in oily sand.
This would explain the over rich exhaust (black tailpipe).
Well after using massive amount of air and beating the filter on some
landscape bricks with textured surface to aid knocking off the gunk.
I washed it in hot water with laundry soap, it smelt Spring Air Fresh...
Dried it and put it in a zip lock bag and poured chainsaw bar oil on
it and worked it in, put it back on the frame and allowed it to sit
overnight, nothing appears to have dripped off it, so either I got it
right or did'nt add enough oil. I poured about 2 oz or so on it, it
seemed to be pretty wet, afterwards I gave it a couple light squeezes
wrapped in papertowels to get the really wet spots thinned out to make
it uniformed.
As for that metal screen, I just do not see how that can restrict air
flow, my goodness it has what maybe 20 or 25 sq inches of surface
area, and its not really that tight of a weave, if it was covered in
dirt sure it would choke off airflow, but that would be enough reason
to investigate whats happening with MPG/sick running bike.
The weave looks tight enough to stop grains of sand, at least in my
neck of the woods we have lots of beach looking sand in the great
lakes area, not so much that dusty desert powder.
Well if the weather clears today I reckon if I find out my bike is too
lean.. Good thing I made a pilot adjusting tool. (Hacked off
screwdriver bit, psst do not even think about using a hacksaw, dremel
or cut off tool with a emery wheel)
Dooden
A15 Green Ape
Oh the battery was low, but not completely dry at least.. charged with
real charger and seemed to be holding just over 13 volts on the bench,
what should this battery have sitting with no charge/load anyway ?
Who is online
Users browsing this forum: No registered users and 18 guests