Folks, as my KLR sits on the gernie awaiting Dr. Schnitz, I decided to
closely examine the airbox ecosystem for intake leaks. I have an
A18/2004 with 20k combat miles. I think it's important to note I'm at
the extreme end of KLR use and abuse. For example, I've been through 7
rear tires, 3 sets of brakes, 2 chains, 3 foot pegs, countless oil and
air filter changes (1,000 miles or less), balancer chain slack
maxed... I'm rough on it as are the conditions I subject it to, so in
many cases your results may/should vary (in a markedly improved way).
(1) The left side drain hole was ground-off 50% and completely missing
das boot (aka rubber duck bill). The cause (according to the flight
data recorder) was attempts to fly early in the KLR's life (jumping).
I'm 155 lbs and even with the shock dialed to firmest, the woops and
launches simply bottomed the rear so hard it caused this (not uncommon)
damage). Quickly you learn it's not a KX! Around 4k miles, I upgraded
to the RL Progressive front/rear suspension and just recently filled
this (left) drain hole with RTV silicone.
(2) The right side das boot is dried-out and now puckered in the
middle, so because it's not fully closed, dirt/dust is getting sucked
into the pre-air filter compartment. So either I have to replace das
boot (p/n 49006-1211, $3) or come up with a way to get this port to
seal but remain drainable.
(3) The end plug (p/n 92066-1211, $4) was missing from the rubber tube
coming from the beather port (note: this port is difficult to get
to/see as it's located AFTER the air cleaner but before the carb inlet
(rubber) duct). This is plug (and issue) is new to me. Somewhere
within the 20k miles it was relieved of its duty. And at the top of
the plastic breather (p/n 14069-1051), the hose was dry-rotted and
leaking. If you remove the entire system and plug one end, no air
should leak when you blow into it. However, mine was dry-rotted and
leaking as was my neighbor's 2006 with 2,600 miles. Looking inside the
air box in the section after the air cleaner, it was a bit dirty. At
the breather port, it's likely some dirt was getting in although there
is a piece of foam filter hanging out of the port (obstructed but best
viewed from left side of bike). In my case, some dirt appears to have
gotten through this little filter. I tugged on it and it won't come
out. It doesn't look serviceable or otherwise replaceable. My thought
here is to clean it and put some tacky filter oil on it. Otherwise, I
just assume remove this entire breather system and plug the hole with a
vinyl cap over the port.
All these drain holes are to assist draining in situations of
flooding. However, I'm curious if any of the rides I've taken in rain,
rivers, etc. would ever have introduced any water into the air box.
Personally, I'd like to see the system tighter than a drum right up to
the air intake port on the rear left side with manual draining
capability. Of course, air does leak in the right side at the hatch
for air filter service, but that could be sealed with a better
gasket/seal (currently foam). So it's possible my intake system was
drawing in some debris due to the plug missing and dry-rotted hose
around the breather. I doubt this is what caused my intake clearances
to retreat so fast in under 5k miles, but at least theoretically it
might have contributed. Inside post-air cleaner compartment, I cleaned
out light dirt or dust, so something has gotten by in the past.
Conclusively, if you haven't checked you air box drains (3 of them), I
suggest you do. Specifically, (1) inspect the two das boots (duck
bills) for damage and proper closure, (2) make sure the breather hose
is properly connected to its drain port on the airbox, (3) make sure
the hose is not dry-rotted and leaking (if so, just snip-off the bad
section and reconnect the breather), and (4) make sure you have a drain
plug or seal-off the bottom end. If you're missing the drain plug like
I was, just fill part of the bottom tube with RTV or something. Then
if you ever need to drain the line just unplug it at the breather.
Personally, this tiny [$4] plug was over-engnineered.
Brian